TA的每日心情 | 擦汗 2019-6-16 23:34 |
---|
签到天数: 1277 天 [LV.10]大乘
|
本帖最后由 冰蚁 于 2016-3-2 10:55 编辑
3 i& l' x9 {" H9 x4 {. G- ^' c5 M c/ `1 D, ?, M
5 S7 ?6 k9 u/ ~, q/ `6 Z' _& U事故经过显示不完全是 google 责任。撞中间是因为 google AV的并道实在太慢了,令人发指的不到 2 mph!!! 导致bus 司机误判了 google AV 并道的企图,想抢先通过。google AV 又回不到原来的道上了,只有并入。结果只有撞了。
* s1 v4 `# \$ n0 C9 G! ?9 \ i/ y% Y e8 D' D8 U, b' u" W2 U. ]
: L1 Z0 B# \% l4 i! g a0 H
, G( M0 G, k, }% O) L$ E A Google Lexus-model autonomous vehicle ("Google AV") was traveling in autonomous mode eastbound on El Camino Real in Mountain View in the far right-hand lane approaching the Castro St. intersection. As the Google AV approached the intersection, it signaled its intent to make a right turn on red onto Castro St. The Google AV then moved to the right-hand side of the lane to pass traffic in the same lane that was stopped at the intersection and proceeding straight. However, the Google AV had to come to a stop and go around sandbags positioned around a storm drain that were blocking its path. When the light turned green, traffic in the lane continued past the Google AV. After a few cars had passed, the Google AV began to proceed back into the center of the lane to pass the sand bags. A public transit bus was approaching from behind. The Google AV test driver saw the bus approaching in the left side mirror but believed the bus would stop or slow to allow the Google AV to continue. Approximately three seconds later, as the Google AV was reentering the center of the lane it made contact with the side of the bus. The Google AV was operating in autonomous mode and traveling at less than 2 mph, and the bus was travelling at about 15 mph at the time of contact.
+ @0 n1 L* v' @! E9 r% ~0 H: P# P# d1 j" S. ?
The Google AV sustained body damage to the left front fender, the left front wheel and one of its driver’s -side sensors. There were no injuries reported at the scene. |
|